Journal of Siberian Federal University. Engineering & Technologies 3 (2013 6) 268-275
УДК 544.6.076.324.2
Methodology to Optimize the Anode Performance
Markus W. Meier and Raymond C. Perruchoud
R&D Carbon Ltd, P.O.Box 362, CH-3960 Sierre, Switzerland
Received 15.05.2013, received in revised form 22.05.2013, accepted 31.05.2013
An aluminium smelter operating its pots with Soederberg technology has experienced a period with a very high number of anode problems, mainly occurring as spikes, hanging anode ends, leak in stud holes, vertical cracks and dusting. The anode problems hindered a planned amperage increase. This paper describes the methodology that was applied to identify the root causes of the problems and to solve them systematically. This methodology includes the following main steps: Initial plant audit; Revamping of equipment causing bottlenecks; Plant capability test; Dynamic process optimization DPO; Validation of improved anode quality and pot performance. By applying this methodology, the anode problems of the smelter could virtually be eliminated. As a consequence the key plant performance figures (current efficiency, carbon consumption, energy consumption and bubble noise) could be improved substantially. This allowed to increase the line current by 7 %.
Keywords: Söderberg paste, plant audit, process optimization, anode quality, anode problems, pot performance.
Introduction
The smelter started up its production in 1971 with VS Soderberg pot technology. In recent years all cells have been upgraded with a closed point feeding system, which has increased the capacity and reduced greenhouse gas emissions. Today the smelter has a nominal capacity of 96'000 tpa.
In 2008 the smelter started to experience a severe crisis with an excessive occurrence of anode problems that peaked in 2009. The main problems were:
- Spikes
- Hanging anode end
- Leak in stud holes
- Vertical cracks
- Dusting.
R&D Carbon was requested to carry out an audit of the carbon plant and the anode performance of the smelter to investigate the root cause(s) of the anode problems.
The audit revealed that the anode quality and pot conditions were interrelated with each other with severe vicious circles, as experienced elsewhere [1]. The presence of carbon dust increased the bath
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temperature and increased bath temperature promoted dusting. Indeed, a very large bath temperature variation from 940 to 1'025 °C could be observed.
The following performance figures defined the status quo in 2009, when the problems were peaking:
- Line current: 113 kA
- Current efficiency: 87,5 %
- Carbon consumption: 540 kgC/tAl
- Anode problems: 0,050/potday
100/week
- Energy consumption: 18,0 kWh/kg.
The methodology of identifying the root causes of the problems and the systematic steps of solving them are described in this document. The subsequent improvement of the anode quality and the influence on the anode performance are also discussed.
Initial Plant Audit
R&D Carbon has conducted a systematic audit of the carbon plant and the anode performance. A key element of the audit was to follow the material stream from the anode raw material intake to the potrooms and take samples at every relevant processing step. These samples were analysed in the laboratory of R&D Carbon for the relevant properties. The comparison of these properties with a vast database allowed to judge each processing step in relation to the worldwide average and benchmark. As a consequence, the potential for improvement could be quantified for every relevant processing step.
The key findings drawn from the audit are discussed hereafter.
Anode Raw Materials
The smelter alternately uses two types of calcined petroleum coke that exhibit different key characteristics. Coke A is a rather coarse and dense material, while coke B exhibits just opposite characteristics. In spite of this, both coke types are principally suitable to produce a high quality anode paste.
The two pitch types being used are compatible with each other and also allow producing a high quality anode paste.
Hence in contrast to other experience [2] the direct influence of the raw material quality as a root cause of the anode problems of the smelter can be excluded.
Anode Paste Production
Three areas with a need for improvement could be identified:
Mixing Energy: A low net mixing energy of 0,6 kWh/t (vs. typically 3 kWh/t) was identified, which has a deleterious effect on the resulting paste quality and anode performance in the pots.
The condition of the continuous BUSS kneader was considered as the main bottleneck in the entire anode production. It was decided to refurbish the kneader with top priority to improve the anode quality.
Dry Aggregate Preparation and Recipe Formulation: The three fractions (coarse 10 - 3,15 mm, intermediate 3,15 - 0,35 mm, fines 2'600 Blaine) were not balanced. The maximum grain size of the
Table I. Anode quality of the smelter in 2008 and worldwide typical Soderberg range
Property Unit Smelter Worldwide typical
Avg. 2s Avg. 2s
App. density green kg/dm3 1,58 0,02 1-57-1,64 0,01
Flowability 1,12 0,03 1,05-1-25 0,05
App. density bakedkg/dm3 1,41 0,04 1,44-1,52 0,03
Spec. electr. resist. mWm 79 6 62-70 4,5
Flexural strength MPa 7,5 1,2 7-11 3,0
Thermal conduct. W/mK 2,4 0,5 2,6-3,4 0,3
Air permeability nPm 30 40 8-18 15
CO2 reactivity residue % 82,6 6,3 80-92 7,0
Air reactivity residue % 56,8 7,7 70-90 7,5
coarse fraction was identified as being too large, the intermediate sizing range too big and the fines fraction being too coarse.
R&D Carbon recommended to re-define the sizing of the coarse fraction to 6,0 - 2,0 mm and the intermediate fraction to 2,0 - 0,0 mm.
Fines Circuit: The fines circuit consists of a horizontal overflow ball mill and a dynamic classifier. The rotor speed of the classifier is kept constant and not used to vary the product fineness.
It was concluded that the fines circuit needed to be addressed specifically prior to a process optimization.
Anode Quality
The following selected key properties were measured on the anode paste and the pilot electrode after baking at 1 000 °C for 5 hours, as shown in Table 1.
Compared to the worldwide typical range, most key properties were substandard and needed improvement. Due to the severity of the anode problems in the pots and the clear assessment of the current situation with the specific identification of the responsible bottlenecks, the smelter decided to refurbish the continuous kneader by the original supplier BUSS AG and pursue the optimization of the paste plant with the technical assistance of R&D Carbon.
Revamping of Equipment Causing Bottlenecks
The refurbishment of the kneader (BUSS K500KE-7D) required the complete replacement and modernization of the main shaft with improved geometry and design (see Fig. 1). Additionally an automated flap gate was installed. With the modernized kneader the paste plant was ready for the stepwise optimization of all relevant processing parameters.
Plant Capability Test
In a first plant capability test, the main goal was to see the influence of parameters such as recipe formulation, dry aggregate temperature, throughput and flap gate position on the specific mixing
- 270 -
Fig;. 1. Refurbished BUSS kneader with reduced shearing gap for Soderberg application and automated flap gate
energy. As a consequence of these trials the specific net mixing energy could be increased from 1.8 up to 3,4 kWh/t, which had a positive effecton the resulting paste quality.
In a second plant capability test, the limitations of the ball mill were quantified. In particular the influence of thr classifier speed fnd the secondary air on tho fines finenets was checked. With tire purpose to produce a paste wioh a high findingf force oh the binder matrix, ohe fines fineoess was increased up to 4'000 Blaine. As the kneader is designed for a considerably higher throughput than the actual throughput of 13,0 t/h, the ball mill turned out to be a bottleneck for the planned process optimPzation.
Dynamic Process Optimization
On behalf of the third plant test the actual dynamic process optimization (DPO) was conducted in October 2010 according to the methodology described in [3]. Three optimization targets were
investigated during the trials:
- Variation of the fines content with standard fines (3 400 Blaine);
- Variation of fines content with finer fines (4 100 Blaine);
- Fine tuning of thermal conditions.
During these trials the specific net mixing energy could be increased from 2,0 to 3,1 kWh/t. As already expected during the plant capability test, the DPO trials were largely limited by the production capacity of the ball mill. Nevertheless, compared to the starting point in 2008 a massive improvement of the paste quality could be obtained with 3'400 Blaine, as shown in Table 2.
Based on the sound test results it was safe to implement the findings of the DPO trials into the routine production which allowed to validate the improved paste quality on full scale in the reduction pots.
Table 2. Improvement of anode quality from 2008 to 2010 (DPO)
Property Unit 2008 DPO in 2010
App. density baked kg/dm3 1,41 1,519
Spec. electr. resistance mWm 79 63
Flexural strength MPa 7,5 11,1
Thermal conductivity W/mK 2,4 3,6
Air permeability nPm 30 12,5
CO2 reactivity residue % 82,6 82,2
Air reactivity residue % 56,8 68,4
Validation of Improved Anode (Quality and Evolution of Performance in Pots
In the first half of 2008 the pot rooms of the smelter were operated at a record high line load of 128.5 kA (average for both lines), after years of increasing in small steps. The number of anode problems had slowly increased, but Orom May 2008 the problems jumped tro a higher level. To couoteract, the line load was reduced to 125 kA, while ihe number of anode problems stabilized at 60 per week. Even lowering the line load to 113 kA (due to the worldwide financial crisis) did not help to reduce the number of anode problems. In fact, the frequency continued to increase to a record high of 100 anode problems per week during teverol months in 2009. When the markets were improving, the line load was again sSepwise inceessed, iuh was nindered to increase aiove 12S kA due to the severe anode situation.
After the improvements had been implemented in the paste plant, the anode performance gradually improved to a very good condition which is sustained even at a level close to record high line load.
It takes the paste 13 to 15 weeks to reach from the anode top the aettom operaring surfacr. However, io took about one etar of pot operatioo with improved paste quelity (ca 4 baking cycles) to reach stable pot performance with a low frequency of 20 anode problems per week (eg 0.01 anode problems per potday).
The Fig. 2 to 6 show how the anode paste quality influenced the number of anode problems, paste consumption,current eoficieocy, specific energy conrumpeion, and line load.
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Fig. 2. Anode problems per week and potday monthly data 2008-2011
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Fig. 3. Anode paste consumption monthly data 2008-2011
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Fig. 4. Current efficiency monthly data 22008 - 22011
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Fig. 5. Energy consumption DC in potrooms mondhly data 2008-2011
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Fig. 6. Line load (avesage of both lines) monthly data 2008-2211
In addition to all improvements of the anode paste, the operation of resetting the anode stubs in the pots was improved in 2010. This also had a positive influence on the overall anode performance.
The accumulated changes made to the anode paste resulted in a different visual appearance of the anode top. A paste produced to a given viscosity target appears visually drier on the anode top today than the same viscosity did before. A new challenge is therefore to adjust the rules and targets for anode top control in such a way that the right viscosity is produced to give optimal results for the baked anodes.
Conclusions
A methodology has been described in this document to systematically optimize the anode performance. The methodology comprises five steps: (1.) initial plant audit, (2.) revamping of equipment causing bottlenecks, (3.) plant capability test, (4.) dynamic process optimization DPO and (5.) validation of improved anode quality and pot performance. The application of the described methodology was illustrated on an actual case of a Soderberg plant [6], but the same methodology can of course also be applied on plants using prebaked anode technology [3, 7].
As for the illustrated case, the close collaboration between the dynamic management and its technical team of the smelter with R&D Carbon was a key factor to not only overcome the severe
crisis, but also to reach performance figures that are near worldwide benchmark.
The described methodology has turned out to be very efficient.
The anode quality and performance in the pots could be improved dramatically:
- Anode problems: from 0.05 to 0.01 per potday (average of all pots) and to 0.00125 per potday in potroom 3;
- Anode paste consumption: from 540 to 485 kgC/tAl;
- Current efficiency: from 87,5 to 90,5 %;
- Energy consumption: from 18,0 to 16,8 kWh/t;
- Bubble noise: doubled.
The massive improvement of these performance figures allowed to increase the line load from 120 to 128,5 kA. The aluminium production cost could be decreased significantly, which has led to a very attractive payback time of the entire project. The combined boost of the line load and current efficiency increase the metal production by 10 %, which corresponds to 9 000 tpa.
References
[1] Rui Oyama Homma // Light Metals. 2000. P. 437-441.
[2] Alexandre Gomes // Light Metals. 1999. P. 497-502.
[3] Raja J. Akhtar, Saleh A. Rabba, Markus W. Meier // Light Metals. 2006. P. 571-575.
[4] Marianne Jensen, Tor Bjarne Pedersen, Kjell Kalgraf // Light Metals. 2007. P. 353-356.
[5] Kjell Kalgraf, Marianne Jensen, Tor Bjarne Pedersen // Light Metals. 2007. P. 357-361.
[6] Nils Einar Saue, Markus W. Meier et al // Light Metals. 2012. P. 1159-1163.
[7] Vinicius Piffer, Markus W. Meier et al. // Light Metals. 2007. P. 959-964.
Методология для оптимизации производительности анода
Markus W. Meier and Raymond C. Perruchoud
R&D Carbon Ltd, P.O. Box 362, CH-3960 Sierre, Switzerland
Алюминиевый завод, работающий с электролизерами Содерберга, пережил период очень больших проблем с анодами, проявляющихся главным образом в появлении конусов, протеков через подштыревые лунки, вертикальных трещин и пенообразования. Проблемы анода затрудняли запланированное увеличение силы тока. Статья описывает методологию, примененную для определения коренных проблем и их систематического решения. Методология включает следующие основные шаги:
- Первичный аудит предприятия;
- Модернизацию оборудования, которое создает узкие места;
- Тестирование возможностей предприятия;
- Динамический процесс оптимизации (ДПО);
- Подтверждение улучшения качества анодов и производительности электролизеров.
С применением этой методики проблема анодов на предприятии может быть фактически устранена. Как следствие, ключевые показатели завода (выход по току, потребление углерода, потребление энергии и пузырьковый шум) могли быть существенно улучшены. Это позволило увеличить ток серии на 7 %.
Ключевые слова: анодная масса, аудит предприятия, процесс оптимизации, качество анода, проблемы анода, производительность электролизеров.